2016년 5월 19일 목요일

Sputum result 2

Sputum result 2

Examination satellite "sputum result 2 (MS-T2)"
Position Tokyo University Institute of Space and Aeronautical Science
The main manufacturer NEC
Official page Examination satellite "sputum result 2 (MS-T2)"
International mark number 1974-008A
Catalogue number 07122
State The operational end
Purpose Confirmation of performance, the electric wave instruction control of the rocket
Examination of the use of geomagnetism posture control
Period of the plan 16th
Design life Two weeks
Launching place Kagoshima outer space observatory
Display machine The M-3C rocket first unit
The launching date and time 1974February 1614:00
Operational end day March 1, 1974
The extinction date and time 1983January 23
Physical good point
Main body dimensions ⌀750mm *450mm
(octagon pillar)
Greatest dimension 1.3m
Mass 56 kg
Posture control system Spin stability method
Orbital element
It is targeted for go-around The earth
Orbit Elliptic orbit
Perigee altitude (hp) 288km
Distant visible point altitude (ha) 3,236km
Orbit angle of inclination (i) 31.2 degrees
Orbit period (P) 121.8 minutes
Deployment apparatus
ヨーヨーデスピナ
Use of geomagnetism spin axial control unit
Keeping magnet

Sputum result 2 (sputum result 2 ごう) is a man-made satellite for the technical examination that Tokyo University Institute of Space and Aeronautical Science (Institute of Space and Astronautical Science in the back, the current Japan Aerospace Exploration Agency space science study headquarters) developed. The development name is MS-T2.

Table of contents

Purpose

Our plane was developed for the purpose of the launching performance test of the M-3C rocket which was the all the paragraphs solid-propellent rocket which Institute of Space and Aeronautical Science developed and the examination of the posture control system of the satellite with the magnetic torquer. I posture controlled it, but the satellite of the laboratory of conventional space was expected only by a spin stability method when more highly precise observation was enabled by using a magnetic torquer method together. This method was adopted in following scientific satellite "たいよう".

Operational

Our plane was launched in the M-3C rocket first unit in (JST) at 14:00 on February 16, 1974 by the Kagoshima outer space observatory and was cast into perigee an altitude of 288km, apogee an altitude of 3,238km, the orbit of orbit angle of inclination 31.2 degrees.

I tested it in orbit until March 1 and finished use because the life of the silver oxide cell which was a power supply ran out.

On January 22, 1983, I broke into the atmosphere and became extinct.

Allied item

Outside link

This article is taken from the Japanese Wikipedia Sputum result 2

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